Midwest Classic Insurance

Visit our community sponsor

Thanks Thanks:  8
Likes Likes:  39
Page 3 of 4 FirstFirst 1234 LastLast
Results 81 to 120 of 153

Thread: the coyote continues to bite... resolved! :)

  1. #81
    Senior Member John Ibele's Avatar
    Join Date
    Sep 2011
    Location
    Minneapolis, MN
    Posts
    719
    Post Thanks / Like
    Bummer, Todd. I was also hoping to see something that would suggest low fuel pressure being the source of the problem. Such a cause could have also been consistent with the temperature dependence (runs for a short bit on cold start). Vapor pressure of the gas would increase with temperature; gasoline starts moving from liquid to vapor phase at about 95F. So if you were suffering from low pressure at some spot in the system, the fuel wouldn't necessarily vaporize immediately, but could at mildly increased temperatures. I would think that would also be consistent with a lean condition interpretation by the ECU.

    I don't see how any of this could be consistent with the free-flowing fuel rail you just demonstrated, and I don't know your engine well enough to comment further. Maybe it will trigger something in the minds of those familiar with your engine. Good luck.
    Last edited by John Ibele; 11-12-2023 at 01:21 PM.
    MK4 #7838: IRS 3.55 TrueTrac T5z Dart 347
    The drawing is from ~7th grade, mid-1970s
    Meandering, leisurely build thread is here

  2. #82
    Member
    Join Date
    Nov 2019
    Location
    Western MA
    Posts
    59
    Post Thanks / Like
    Quote Originally Posted by toadster View Post
    all vacuum ports are either plugged or routed to things like vacuum assist brakes
    Have you verified that the brake booster holds vacuum?
    MK IV #8639, 347/T5

  3. #83
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    Quote Originally Posted by jab351w View Post
    Have you verified that the brake booster holds vacuum?
    yes tested this - holds a strong vacuum
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  4. #84
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    Quote Originally Posted by JeffP View Post
    I saw your purple wire there.. I'm assuming you did the Tach wire to one of those coil overs - sure thats all clean and correct?
    correct - haven’t reattached the tachometer wire yet
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  5. #85
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    Quote Originally Posted by Its Bruce View Post
    Observations:

    1. Your MAP spikes to atmospheric (100kpa) whenever you're applying throttle and you're only applying 25% max throttle. This is consistent in both logs.
    2. On the first log, your O2's seem to be adjusting STFT's as they should. I see nothing immediately wrong with their operation, but I don't see where you're monitoring the O2 mV for each bank.
    3. Your trouble codes are all symmetric except for P2008. Is there a Bank 2 for this code?
    4. The fuel rail pressure gets up to >3,000psi with the O2's disconnected but only ~1,000psi in the initial log.
    5. Your Fuel System #1 Status with the O2's plugged in is still "CL - Fault" status.


    Is the MAP sensor the correct PN? Is it a 1 bar MAP? Is it installed in the correct location?

    Take a look here for some info on the CL - Fault status: https://forum.hptuners.com/showthrea...e-Turbo-Advice

    thanks for the eyeballs on the log

    #1 good for consistency
    #2 I can check mV in logging - was trying to grab as much as possible
    #3 agree on symmetry for codes nothing from LUND on the same question I had
    #4 fuel pressure seems to throttle back quite a bit, most likely a Safety precaution
    #5 this is the perplexing part, two separate o2 harnesses same issue

    the map sensor is from the control pack, Lund said it was tracking well for a non stock intake setup
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  6. #86
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    ok - we did some off the wall testing tonight, thanks to my buddy Sean who've I've known for 25+ years...

    he was here when the kit arrived, and hasn't seen the car in a while, so we went through our testing cycles, going through all the parts replaced, etc. pretty much relived this thread

    we started talking about the direct injection and port injection on this engine, we hadn't checked the wiring to the lower (direct) injectors so we got out the boroscope and looked around, didn't see anything disconnected or any rodent damage
    after a while, he said 'what if we disconnect the bank #2 injectors on top' - we figured it would be worth a try, since the other injectors would add some fuel to run as well

    what do you know - the engine fired up and idled just fine, a few loud bangs, and the driver side got nice and hot! the bangs were excess gas in the cylinders relieving themselves
    the look on my face must have been something else because we all started laughing, not thinking that the engine would work properly with injectors #5,6,7,8 unplugged - we were perplexed, yet somewhat relieved...

    so what did that mean?

    we tested with all 4 injectors disconnected, O2 readings were good, so we started a process of elimination

    plugged in injector #5 and started the engine, O2 readings are good, temps coming up
    plugged in injector #5 and #6 and, same goodness
    we then additionally plugged in #7, so we had 5,6,7 plugged in, O2 readings are good! temps coming up!
    then we plugged in #8, thinking - maybe it was just a fluke, NOPE - O2 readings went bad - so we determined that injector #8 must be stuck open!

    unplugged #8 and it ran fine again... so tomorrow, going to the store to find a replacement injector...

    what's really perplexing here is no codes led us to an injector!!

    I'll definitely be changing the oil as it reeks of gasoline and has probably lost a lot of it's lubricity
    leave it to me to be a guy who changes his oil before he puts a mile on his car...

    fingers crossed, a new injector will remedy this!!!
    I believe it's the MOTORCRAFT CM5269

    here's a pic of my buddy Sean and my son Ryan when we first got the kit, it's been a journey!

    Last edited by toadster; 11-14-2023 at 12:38 AM.
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  7. Likes Ted G, Ducky2009 liked this post
  8. #87
    Senior Member
    Join Date
    Feb 2012
    Location
    Prescott, AZ
    Posts
    669
    Post Thanks / Like
    Wow, good news but good grief, a stuck open injector? I am so glad that you are finally moving forward with probable solution.
    Get a good nights sleep, a new injector, and ones hopes put this saga to rest.
    Once you are sure of the failure, I think a long talk with Ford Performance is in store. I mean with all the troubleshooting hours you have put into your effort, they should trade your bad injector for some kind of compensation like extending the warranty period on your crate engine.
    MK4 base kit, 2004 Mach 1 donor, 4.6L DOHC, TR-3650 5-speed, narrowed stock axle with 3.55 gears and TruTrac, PS, PB, ABS, 17" Halibrand replica wheels, started 12/2011, registered 9/2014, sold 3/1/2018.
    1970 Mustang Fastback Coyote powered Boss 302 tribute. Started 10/14/16.
    Gen 3 Coupe Base Kit non-donor build. Ordered 4/5/2024 to be received August 2024.

  9. Likes Ted G liked this post
  10. #88
    Senior Member Nigel Allen's Avatar
    Join Date
    Oct 2012
    Location
    South Australia
    Posts
    504
    Post Thanks / Like
    Quote Originally Posted by toadster View Post
    ok - we did some off the wall testing tonight, thanks to my buddy Sean who've I've known for 25+ years...

    he was here when the kit arrived, and hasn't seen the car in a while, so we went through our testing cycles, going through all the parts replaced, etc. pretty much relived this thread

    we started talking about the direct injection and port injection on this engine, we hadn't checked the wiring to the lower (direct) injectors so we got out the boroscope and looked around, didn't see anything disconnected or any rodent damage
    after a while, he said 'what if we disconnect the bank #2 injectors on top' - we figured it would be worth a try, since the other injectors would add some fuel to run as well

    what do you know - the engine fired up and idled just fine, a few loud bangs, and the driver side got nice and hot! the bangs were excess gas in the cylinders relieving themselves
    the look on my face must have been something else because we all started laughing, not thinking that the engine would work properly with injectors #5,6,7,8 unplugged - we were perplexed, yet somewhat relieved...

    so what did that mean?

    we tested with all 4 injectors disconnected, O2 readings were good, so we started a process of elimination

    plugged in injector #5 and started the engine, O2 readings are good, temps coming up
    plugged in injector #5 and #6 and, same goodness
    we then additionally plugged in #7, so we had 5,6,7 plugged in, O2 readings are good! temps coming up!
    then we plugged in #8, thinking - maybe it was just a fluke, NOPE - O2 readings went bad - so we determined that injector #8 must be stuck open!

    unplugged #8 and it ran fine again... so tomorrow, going to the store to find a replacement injector...

    what's really perplexing here is no codes led us to an injector!!

    I'll definitely be changing the oil as it reeks of gasoline and has probably lost a lot of it's lubricity
    leave it to me to be a guy who changes his oil before he puts a mile on his car...

    fingers crossed, a new injector will remedy this!!!
    I believe it's the MOTORCRAFT CM5269

    here's a pic of my buddy Sean and my son Ryan when we first got the kit, it's been a journey!

    G'day Todd,

    Well done! There is a stack of people in this community breathing a sigh of relief for you.

    Onward and upward.

    Cheers,

    Nige
    Mk.4 FFR supplied Right hand drive
    Received 12/2012 completed 12/2019
    Gen1 Coyote / TKO600 / IRS
    Lots of mods to make compliant for Australian design rules

  11. #89
    Senior Member
    Join Date
    Aug 2021
    Location
    Moyock, NC (OBX/Hampton Roads)
    Posts
    399
    Post Thanks / Like
    A lot of speculation about debris in the fuel rail on this thread, I wonder if thats the issue after all that caused the injector to be stuck?
    MK4 Complete Kit #10315 / Coyote G3 / TKX / 427 HardTop
    Build Thread Production Date: 2/26/22, Registered 5/19/22, Graduated 3/1/2023

  12. #90
    Senior Member
    Join Date
    Aug 2019
    Location
    Paradise/Magalia Ca
    Posts
    187
    Post Thanks / Like
    It sounded like a mechanical issue hope it solves everything

  13. #91
    Senior Member Tooth's Avatar
    Join Date
    Nov 2020
    Posts
    205
    Post Thanks / Like
    I can't believe how patient you've been with this. I really hope this is it.
    Mark IV Gen 3 Coyote
    Started 7/22.

  14. #92
    Senior Member Mastertech5's Avatar
    Join Date
    Jul 2020
    Location
    Spencer, MA
    Posts
    865
    Post Thanks / Like
    Glad to hear it, you finally got it.
    33 Hot Rod Stage 1, Gen.2 ordered 11/11/2021 started June 12, 2022, LS3 E-Rod crate engine, Tremec TKX, 8.8 WITH 3.55 Ratio and limited slip with 31 spline axles.17X8 and18x10 Race Star wheels wrapped in Conti Extreme contact DWS tires, Mustang Cobra brakes all around. Electric PS and AC. Hard top, electric windows and bike fenders. First Start 5/31/2023. Go-Kart 6/2/2023.

  15. #93
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    Quote Originally Posted by JeffP View Post
    A lot of speculation about debris in the fuel rail on this thread, I wonder if thats the issue after all that caused the injector to be stuck?
    we thought the same thing... I almost swapped around injectors when I pulled off the fuel rail, it would have moved the issue around - but we had no clue until we tested like this
    what's odd is that the injector 'clicked' when we applied 12v - and no codes from the ECU on this issue...

    Quote Originally Posted by jamminj View Post
    It sounded like a mechanical issue hope it solves everything
    Quote Originally Posted by Tooth View Post
    I can't believe how patient you've been with this. I really hope this is it.
    Quote Originally Posted by Nigel Allen View Post
    G'day Todd,

    Well done! There is a stack of people in this community breathing a sigh of relief for you.

    Onward and upward.

    Cheers,

    Nige
    Quote Originally Posted by Alan_C View Post
    Wow, good news but good grief, a stuck open injector? I am so glad that you are finally moving forward with probable solution.
    Get a good nights sleep, a new injector, and ones hopes put this saga to rest.
    Once you are sure of the failure, I think a long talk with Ford Performance is in store. I mean with all the troubleshooting hours you have put into your effort, they should trade your bad injector for some kind of compensation like extending the warranty period on your crate engine.
    appreciate all of your inputs, it's been a slog, praying a new injector will remedy this once and for all!
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  16. #94
    Senior Member
    Join Date
    Apr 2017
    Posts
    482
    Post Thanks / Like
    Man, what an ordeal. Great detective work on it!! Hope the new injector gets it solved! Seems like Ford owes you something for sure.

  17. #95
    Senior Member
    Join Date
    Mar 2011
    Location
    Heart of Dixie, Alabama
    Posts
    1,857
    Post Thanks / Like
    After reading your fuel rail post, I thought, surely he swapped sides with the inj to see if the problem moved.
    Anyway, celebrating here for your success.
    I am going to call it fixed. I know you are kicking your heels up.
    20th Anniversary Mk IV, A50XS Coyote, TKO 600, Trunk Drop Box, Trunk Battery Box, Cubby Hole, Seat Heaters, Radiator hanger and shroud.

  18. #96
    On a roll Al_C's Avatar
    Join Date
    Aug 2014
    Location
    Wheaton, IL
    Posts
    1,415
    Post Thanks / Like
    I, too, am thankful you solved it. I knew it had to be fuel related, but who'd have thought it was a single injector! I think everyone watching this thread has benefitted from your experience. I'm sorry you had to go through all this, but you've helped a lot of folks here with the details you've shared!
    Mk IV Roadster - #8650 - delivered 7-17-2015 - first start 7-28-2018 - first go-kart 10-13-2018 - licensed and on the road 9-9-19: body/paint completed 3-17-2020.
    Complete kit / 2015 Coyote / TKO600 / IRS / Wilwood brakes / Mid-Shift mod / Power Steering / Heater and Seat Heaters / RT turn signal / Breeze radiator shroud and mount

  19. #97
    Ted G's Avatar
    Join Date
    Aug 2021
    Location
    El Dorado Hills, CA
    Posts
    762
    Post Thanks / Like
    Full disclosure Todd..... I did not drive by your house for at least the past week or so just to send you some good Joo Joo; or at least keep away the bad. If this works, you may owe me a beer or better yet, a killer Cabernet!

    Ted

  20. Likes toadster liked this post
  21. #98
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    Quote Originally Posted by Ted G View Post
    Full disclosure Todd..... I did not drive by your house for at least the past week or so just to send you some good Joo Joo; or at least keep away the bad. If this works, you may owe me a beer or better yet, a killer Cabernet!

    Ted

    LOL I've got both!
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  22. Likes Ted G liked this post
  23. #99
    Senior Member
    Join Date
    Jun 2023
    Location
    Tonganoxie KS
    Posts
    137
    Post Thanks / Like
    I had been watching this thread intently. I am glad you solved the problem. If it makes you feel better I am going to change my oil before I drive the car too.

  24. Likes toadster liked this post
  25. #100
    Senior Member Lidodrip's Avatar
    Join Date
    May 2020
    Location
    Yarmouth, Maine
    Posts
    261
    Post Thanks / Like
    Very happy that you solved the problem, I think it is fair to say you now have a Master's degree in trouble shooting the Coyote. Strong work!

    James
    Mk4 Roadster #9974 - Picked Up 1/2021. Complete kit, Gen 2 Ford Coyote / TKX, IRS. Completed 9/2023

  26. #101
    Junior Member
    Join Date
    Nov 2023
    Posts
    4
    Post Thanks / Like
    All,

    Quick Intro : I'm the Sean that had the crazy idea to unplug the injectors and "let's see what happens".
    I have to second what Todd said : The look on his face when it fired up without the port injectors plugged in was PRICELESS!.

    I'm talking to todd now. He needs a priest. He replaced the injector, and still has the same problem.

    If he unplugs ANY single injector, the seems to work, . If all eight are plugged in, the Bank 2 basically shuts down.

    Anyone got any ideas ? It's either a fuel delivery problem, or not enough power to run EVERYTHING plugged in.

    Sean
    Last edited by spm97; 11-14-2023 at 09:31 PM.

  27. #102
    JohnK's Avatar
    Join Date
    Sep 2018
    Location
    SF Bay Area, CA
    Posts
    2,222
    Post Thanks / Like
    Quote Originally Posted by spm97 View Post
    He replaced the injector, and still has the same problem.

    If he unplugs ANY single injector, the seems to work, . If all eight are plugged in, the Bank 2 basically shuts down.
    That's very interesting (though I'm sure also pretty infuriating for poor Todd). That's a very significant additional clue. I have no idea what it means, but I'm guessing someone more familiar with the coyote, like Ford Performance or Lund, would find this additional information pretty useful. Hopefully the root cause is not too far away now.

    Maybe not enough engine grounds? (JUST KIDDING !)
    MkIV Roadster build: Gen 2 Coyote, IRS, TKO600. Ordered 10/24/18. Delivered 1/29/19. Engine installed 8/8/21. First start 9/12/21. First go-kart 9/17/21. Off to paint 4/11/22. Back from paint 12/30/22. Build thread here.

  28. Likes toadster liked this post
  29. #103
    Senior Member
    Join Date
    Mar 2011
    Location
    Heart of Dixie, Alabama
    Posts
    1,857
    Post Thanks / Like
    The 4th injector takes the fuel ratio out of range for the O2 system. Too much fuel, as measured by the O2. Are the injectors on the bad side the same color as the other side? Does the noid light seem to pulse the same from one band to the other.
    Do not know how, but could the bad side be batch firing the injectors. I am sure the Coyote is sequentially fired injectors.
    Just guessing?
    20th Anniversary Mk IV, A50XS Coyote, TKO 600, Trunk Drop Box, Trunk Battery Box, Cubby Hole, Seat Heaters, Radiator hanger and shroud.

  30. #104
    Senior Member
    Join Date
    Feb 2012
    Location
    Prescott, AZ
    Posts
    669
    Post Thanks / Like
    Quote Originally Posted by spm97 View Post
    All,

    Quick Intro : I'm the Sean that had the crazy idea to unplug the injectors and "let's see what happens".
    I have to second what Todd said : The look on his face when it fired up without the port injectors plugged in was PRICELESS!.

    I'm talking to todd now. He needs a priest. He replaced the injector, and still has the same problem.

    If he unplugs ANY single injector, the seems to work, . If all eight are plugged in, the Bank 2 basically shuts down.

    Anyone got any ideas ? It's either a fuel delivery problem, or not enough power to run EVERYTHING plugged in.

    Sean
    Well this is one for Ford Performance to step up and solve now. They need the engine back so that they can resolve their issue. The best thing that Ford Performance can do is warranty replace the engine with a new crate engine and let Todd move on with his life. Yes, the engine needs a exorcist, maybe Todd too as these demons have to left their mark.
    MK4 base kit, 2004 Mach 1 donor, 4.6L DOHC, TR-3650 5-speed, narrowed stock axle with 3.55 gears and TruTrac, PS, PB, ABS, 17" Halibrand replica wheels, started 12/2011, registered 9/2014, sold 3/1/2018.
    1970 Mustang Fastback Coyote powered Boss 302 tribute. Started 10/14/16.
    Gen 3 Coupe Base Kit non-donor build. Ordered 4/5/2024 to be received August 2024.

  31. #105
    Not a waxer Jeff Kleiner's Avatar
    Join Date
    Feb 2011
    Location
    Bloomington, Indiana
    Posts
    8,094
    Post Thanks / Like
    Quote Originally Posted by Alan_C View Post
    Well this is one for Ford Performance to step up and solve now. They need the engine back so that they can resolve their issue. The best thing that Ford Performance can do is warranty replace the engine with a new crate engine and let Todd move on with his life. Yes, the engine needs a exorcist, maybe Todd too as these demons have to left their mark.
    I have to disagree Alan. I can’t see this as an engine hard parts problem; it’s electrical or fuel related.

    Jeff

  32. Likes toadster liked this post
  33. #106
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    update from what Sean mentioned...

    i replaced injector #8, same issue O2 goes to max lean
    unplug injector #8, O2 issue goes away

    Sean asked to unplug injector #7, so all others plugged in - pulled #7, O2 issue goes away, plug back in O2 issue comes back
    to further test, I pulled injector #1 (on bank 1), with all others plugged in, O2 issue (on bank#2) goes away

    so it seems that having all 8 injectors plugged in (electrically) the O2 issue occurs on bank #2

    it's always bank #2 O2 issues, never bank #1
    the O2 issue only occurs when all 8 injectors are plugged in
    the O2 issue goes away when just one of the injectors is unplugged
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  34. #107
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    also, we were thinking possibly the fuel rail maybe wasn't feeding the whole way back to cylinder #8, maybe not blocked but maybe a restriction, so I upped the physical FPR to 71 psi (above the 65psi base) and didn't change the issue

    since I know the engine is grounded, I'll go back and check the 12V feeds and redo them
    super stumped
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  35. #108
    Senior Member Mastertech5's Avatar
    Join Date
    Jul 2020
    Location
    Spencer, MA
    Posts
    865
    Post Thanks / Like
    Try plugging in the old #8 injector on the connector of the one you dissconnect and see what happens. It won't be connected to fuel so if it runs bad then you definitely have an electrical issue. If it runs good, fuel.
    33 Hot Rod Stage 1, Gen.2 ordered 11/11/2021 started June 12, 2022, LS3 E-Rod crate engine, Tremec TKX, 8.8 WITH 3.55 Ratio and limited slip with 31 spline axles.17X8 and18x10 Race Star wheels wrapped in Conti Extreme contact DWS tires, Mustang Cobra brakes all around. Electric PS and AC. Hard top, electric windows and bike fenders. First Start 5/31/2023. Go-Kart 6/2/2023.

  36. Likes Railroad liked this post
  37. #109
    Senior Member J R Jones's Avatar
    Join Date
    Mar 2021
    Location
    SE WI Kettle Moraine
    Posts
    1,173
    Post Thanks / Like
    Quote Originally Posted by toadster View Post
    update from what Sean mentioned...

    i replaced injector #8, same issue O2 goes to max lean
    unplug injector #8, O2 issue goes away

    Sean asked to unplug injector #7, so all others plugged in - pulled #7, O2 issue goes away, plug back in O2 issue comes back
    to further test, I pulled injector #1 (on bank 1), with all others plugged in, O2 issue (on bank#2) goes away

    so it seems that having all 8 injectors plugged in (electrically) the O2 issue occurs on bank #2

    it's always bank #2 O2 issues, never bank #1
    the O2 issue only occurs when all 8 injectors are plugged in
    the O2 issue goes away when just one of the injectors is unplugged
    T,
    This is almost identical to my experience posted here on 10-30. That was a C4 Corvette and I too got all the "fix the ground" suggestions.
    In that case the injectors are constant 12V and (each bank) gets switched to ground. I went for the ground signal coming out of the ECU, and it was not there. That was a simple system compared to your Coyote and a new ECU fixed it.
    jim

  38. #110
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    Quote Originally Posted by J R Jones View Post
    T,
    This is almost identical to my experience posted here on 10-30. That was a C4 Corvette and I too got all the "fix the ground" suggestions.
    In that case the injectors are constant 12V and (each bank) gets switched to ground. I went for the ground signal coming out of the ECU, and it was not there. That was a simple system compared to your Coyote and a new ECU fixed it.
    jim
    yes, this is my concern as we're on a 2nd ECU and 2nd engine harness...

    the only part that hasn't been replaced is the PDU harness which I'm wondering if it may be causing the electrical issues, so I'll be verifying all those connections
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  39. #111
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    Quote Originally Posted by Mastertech5 View Post
    Try plugging in the old #8 injector on the connector of the one you dissconnect and see what happens. It won't be connected to fuel so if it runs bad then you definitely have an electrical issue. If it runs good, fuel.
    we tested this last night, the injector plugged into the harness didn't seem to cycle when we ran the engine
    and the engine still triggered bank #2 O2 when all 8 injectors plugged in

    we still get a clean O2 reading when 7 of 8 injectors are plugged in, but when all 8 injectors are plugged in it triggers the O2

    still on the path that this could be an electrical issue... only thing we haven't swapped out is the PDU for the Control Pack
    Ford states it shouldn't cause any issues with O2, but given this is the power unit for the control pack, I'm starting to think it may be one more thing to test/replace?
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  40. #112
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    if anyone is interested I have my HP Tuner logs here: https://drive.google.com/drive/folde...qf?usp=sharing
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  41. #113
    Senior Member
    Join Date
    Feb 2012
    Location
    Prescott, AZ
    Posts
    669
    Post Thanks / Like
    What has been your communication with Ford Performance? With all that you have been through, it is time they just stood tall and replace the crate engine, controls pack, engine and body harnesses. You have gone so far beyond what normal troubleshooting should require. As much as I believe you want to fix it, diminishing returns and just more delays.
    MK4 base kit, 2004 Mach 1 donor, 4.6L DOHC, TR-3650 5-speed, narrowed stock axle with 3.55 gears and TruTrac, PS, PB, ABS, 17" Halibrand replica wheels, started 12/2011, registered 9/2014, sold 3/1/2018.
    1970 Mustang Fastback Coyote powered Boss 302 tribute. Started 10/14/16.
    Gen 3 Coupe Base Kit non-donor build. Ordered 4/5/2024 to be received August 2024.

  42. #114
    Senior Member Mastertech5's Avatar
    Join Date
    Jul 2020
    Location
    Spencer, MA
    Posts
    865
    Post Thanks / Like
    The O2 sensors shouldn't even affect how the the engine runs until you get into closed loop, about when the coolant hits 160 degrees. This is all very wierd! There's one thing that bugs me about Ford. They use all these acronyms and don't really give you a index to see what they stand for. So with that said, what's the PDU?
    33 Hot Rod Stage 1, Gen.2 ordered 11/11/2021 started June 12, 2022, LS3 E-Rod crate engine, Tremec TKX, 8.8 WITH 3.55 Ratio and limited slip with 31 spline axles.17X8 and18x10 Race Star wheels wrapped in Conti Extreme contact DWS tires, Mustang Cobra brakes all around. Electric PS and AC. Hard top, electric windows and bike fenders. First Start 5/31/2023. Go-Kart 6/2/2023.

  43. Likes J R Jones liked this post
  44. #115
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    Quote Originally Posted by Alan_C View Post
    What has been your communication with Ford Performance? With all that you have been through, it is time they just stood tall and replace the crate engine, controls pack, engine and body harnesses. You have gone so far beyond what normal troubleshooting should require. As much as I believe you want to fix it, diminishing returns and just more delays.
    yep we were testing the PDU harness tonight, figured out which fuses feed the injectors, COPs, etc... still nothing...

    Quote Originally Posted by Mastertech5 View Post
    The O2 sensors shouldn't even affect how the the engine runs until you get into closed loop, about when the coolant hits 160 degrees. This is all very wierd! There's one thing that bugs me about Ford. They use all these acronyms and don't really give you a index to see what they stand for. So with that said, what's the PDU?
    PDU = Power Distribution Unit - e.g. the fuse box with the 250A bussman fuse

    feels like we're chasing a ghost... need an electrical exorcist!
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

  45. #116
    Junior Member
    Join Date
    Nov 2023
    Posts
    4
    Post Thanks / Like
    Hey all,
    Does anyone have a detailed pinout of the Fuse Box ? From what we can tell, fuses 1 thru 4 will get power once the engine is "started" (they do NOT have power with just the key on - something must "Enable" them). If anyone can tell me how they get powered, that would help.
    The supply for fuses 1 thru 4 seems to be connected, which makes sense if it's the output from a relay. Which relay ?

    Can someone please confirm with the key just in the "On" position, if you put a voltmeter between the wire that is common to all the injectors (i think it was a blue/gray color) and ground you have 0 volts.

    We figured out the Fuse1 goes to the PDU harness pins 1,2,13, and one of the pins in the third connector (can't remember it's name).

    It _Appears_ that Fuse 2 and Fuse 4 go to the larger connector with 4 wires (3 of the 4 pins on the outside have a heavier gauge wire, and one of the small center pins is used, and then there are a lot of unused small pins) that T's off the PDU harness right before the ECU. one of those 4 wires _Appears_ to be the +12V for the Coils, and one of those 4 wires _Appears_ to be the +12V for the Cam Solenoids, which I believe are fuse #2 and Fuse #4. Again, it someone could confirm that, it would be appreciated.

    The remaining larger wire on that connector APPEARS to be the +12V for the injectors, but the weird thing is it is connected to the "Supply" side of Fuses 1-4. And we never found anything connected to the load side of Fuse #3 (at least before I left).

    I think something is screwy with the +12V for the injectors. It makes no sense that (again - from the best I could tell) they are all connected to the Supply side of fuses 1 thru 4.

    Anyway, that's my thoughts from the evening. Hopefully this helps give people ideas.

    Sean

  46. #117
    East Coast Speed Machines Erik W. Treves's Avatar
    Join Date
    Feb 2011
    Location
    Huntsville, Al
    Posts
    2,109
    Post Thanks / Like
    your logs clearly show Bank 2 as lean - no fuel on start or 30 seconds in and then recovers fine.

    your logs aren't logging enough data to provide any more info....

    your cams are good as is timing.... your DI pressure looks ok - but I don't see fuel injector PW - the MAF and air load look good as well

    Are you sure the MAF isn't in there backwards?

    it definitely clears up though - are you sure you don't have an exhaust leak in front of the O2 on bank 2? it is basically showing LEAN the entire time but trims are good.... have you checked voltage at that O2?? it seems to be ok on start then checks out.

    I would look really closely at the fuel injectors and flush out the fuel rail to make sure you don't have any debris that made it to the injectors - then swap them to the other side bank...
    Last edited by Erik W. Treves; 11-17-2023 at 09:01 AM.
    FFR 1879, Blown DSS 306,REDLINE management, VeryCoolParts Tuned 460RWHP

    FFR 818S, The Flash, Chassis #5, 2.0L, LSD, Electromotive TEC-S, VCP Tuned, 278RWHP 265 RWTQ

    FFR 6651, Green Lantern, 408W Crate, Hellion 66mm Turbo, JGS Waste gate / Blowoff valve, Tec-GT management, VCP Tuned, 575 RWHP, 690 RWTQ

    FFR 8335, Black Mamba, 289 FIA CSX 2001 tribute car, 347, 48 IDA webers, VCP Tuned, 311 RWHP 386 RWTQ, 3-link, Trigo's

    FFR 0004, Gen 3 , Hawk Coupe, Coyote twin turbo, 683 RWHP 559 RWTQ, IRS, VCP Tuned. "not too shabby"

    US ARMY Maintenance Test Pilot (CW4 Retired)

  47. #118
    Senior Member
    Join Date
    Mar 2011
    Location
    Heart of Dixie, Alabama
    Posts
    1,857
    Post Thanks / Like
    I would see if I could get Ford to approve and pay for a scan at a Ford dealer. Their equipment is unreal for the amount of data that is accessible.
    It also can show a history, hopefully on crate engine ECU's also.
    If the Ford hotline is really concerned about the issue, I feel this would be an easy choice for them.
    I would take stan97 with me, if it happens.
    20th Anniversary Mk IV, A50XS Coyote, TKO 600, Trunk Drop Box, Trunk Battery Box, Cubby Hole, Seat Heaters, Radiator hanger and shroud.

  48. #119
    David aka Ducky2009 Ducky2009's Avatar
    Join Date
    Dec 2016
    Location
    Lilburn, GA
    Posts
    775
    Post Thanks / Like
    Quote Originally Posted by toadster View Post
    also, we were thinking possibly the fuel rail maybe wasn't feeding the whole way back to cylinder #8, maybe not blocked but maybe a restriction, so I upped the physical FPR to 71 psi (above the 65psi base) and didn't change the issue
    Is it possible that the gauge is defective and you're getting too much pressure? Have you tried turning the fuel pressure down?
    MK4 Build #9035 Delivered 2/17/17, First Start & Go-Kart 6/2/17, Licensed 9/1/17
    Paint - Lightning Blue Metallic, No Hood Scoop, No Stripes
    Gen 2 Coyote Engine & TKO-600. Solid Axle, 8.8-3.55, Power Steering, Power Brakes, Dual Roll Bars
    Heater and Glove Box, Drop Trunk, Wipers, Radio, FFR Vintage Gauges, Custom Dash
    Build Thread: http://thefactoryfiveforum.com/showt...MK4-Build-9035

  49. #120
    25th Anniversary #9772 toadster's Avatar
    Join Date
    May 2011
    Location
    Folsom, CA
    Posts
    1,793
    Post Thanks / Like
    Quote Originally Posted by Ducky2009 View Post
    Is it possible that the gauge is defective and you're getting too much pressure? Have you tried turning the fuel pressure down?
    checked with gauge and with the computer, they're in sync - i trusted the measurement, so I removed the FPR gauge and just running off the ECU measurements
    Todd
    25th Anniversary MkIV | #20 of 25 | Build #9772
    https://cobradreams.com/ <- my build!

Page 3 of 4 FirstFirst 1234 LastLast

Tags for this Thread

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •  

Stewart Transport

Visit our community sponsor