The testing of possible combinations for upgrading the challenge series for 2012 was started last weekend at VIR. This first test involved an entire engine upper end package from Trick Flow as well as an upgraded front suspension with new geometry and a front anti-roll bar. The front brakes were also uprgraded to handle the added power as well.
Upgrades tested:
Trickflow top end package: TFS-K514-360350B with the intake swapped for an "R Series"
7/8" front anti-roll bar
FFR MKIV front spindles
1994-1998 Mustang Cobra front brakes
3:27 rear axle ratio
Larger Mass Air/Throttle/Injectors
This is a package very similiar to the one used to win the 2007 NASA ST2 National chapionship by Tony Buffamonte. (He had Brembo fron Calipers and double adjustable shocks as well)
Testing Summary:
Installation: Intallation time for this test was very rushed as we had just returned from Mid-Ohio the prior weekend. As soon as we pulled in to Factory Five on Monday night we unloaded the car and immediately began tearing down the engine and front suspension. The top-end switchover included a cam change so the balancer and timing cover had to be removed along with the oil pan. Other than a leak from the pan gasket being rushed the entire swap went smoothly and the engine fired up right away with a new Mass air meter and 24lb injectors but no changes to the factory compluter.
The front suspension also went together relatively easy once the updated MKIV style upper arm mount was welded into place, this was the only fabrication required in the changeover. The anti-roll bar was designed to be a bolt on and with some minor tweaks to the brackets and a change to longer lower shock bolts it bolted right up to the front of the main frame rails. (it is high enough to clear the tie down hooks on newer cars).
After some minor set up work, timing and fuel pressure were set conservatively, aligmnent, and hitting the scales the car was loaded back on the truck on Wed to head down to VIR.
Friday at the track was planned for sorting the car out while John George ran Ed Boothman's car in the Grassroots Motorsports Ultimate Track Car Challenge. Most of Friday was spent chasing gremlins as the oil pan gasket was leaking rather obscenely and the data acq system was not allowing the car to get past 5000 rpm. We ended up losing 3 of the 4 sessions friday getting the pan gasket replaced and chasing the engine miss but by Saturday morning we were back in buisiness and ready for testing.
Our weekend testing sessions were run in the Time Trials group with NASA, probably a mistake since the sessions are very short and we were being cautious to not interfere with people when they were on their hot laps. However we were able to get some very good first impressions and comparisons as well as figure out what still needs time sorting out.
Notes and observations from the test:
Weather was very hot and humid, low 100s, but my oem 1996 Mustang radiator was still enough to cool with the higher HP.
Spring rates were left at 750/525 to start, with the sway bar this gave some push but not a lot, try lowering to 700 front for next round
Brake pedal was harder due to smaller caliper volume. Effort was still acceptable but for a car already on the high side a smaller master would be better
Brake bias needed more adjustment but was also very close, possibly use just a bit more front bias.
Tested 2:73 gears and 3:27s (in second car with same engine combo) 2:73s do not work well with higher rpm power peak. 3:27s worked well even on the long VIR backstraight and we did not run out of rpm.
Overall balance of the car felt very similiar, coming out of corners was the same just instead of having to shift at 5000 rpm that is where the car really took off.
Top speeds on the long straights went up by about 6-8mph from 128-129 to around 136
Sound of the car was completely different, even at the same rpms there was more of a growl, at 6000 rpm it was even better
Did not get to dyno but did race the 85 car (320 hp at the wheels) down the backstraight and cars ran just about identical
Still need to dial in the outer tie rod height (shims or spacers) as there was some roll steer that needs to be dialed out.
Summary: Overall we could have used more time but it was a good first test. The car is much quicker down the straights but the power does not change the overall balance. Lap times were 3-4 seconds quicker than we were at the same event last year (very similiar conditions) but with more testing there is likely at least 1 more second worth of time to come. Most of this from dialing in the brake bias and tweeking the spring rates. Also the engine was tuned very conservatively because we did not have time to get an air fuel reading so fuel pressure was set at 52 and timing at 14. The 3:27 gears also made the car much more fun than the 2:73s.
Overall the test was a success and all 3 drivers who drove it thought it was a marked improvement from the current configuration.